{"id":4962,"date":"2019-05-27T19:32:51","date_gmt":"2019-05-27T23:32:51","guid":{"rendered":"http:\/\/mikestrawbridge.com\/blog\/?p=4962"},"modified":"2019-06-14T22:10:44","modified_gmt":"2019-06-15T02:10:44","slug":"porsche-944-torque-tube-bearings","status":"publish","type":"post","link":"http:\/\/mikestrawbridge.com\/blog\/2019\/05\/porsche-944-torque-tube-bearings\/","title":{"rendered":"Porsche 944 Torque Tube Bearings"},"content":{"rendered":"\n<h4 class=\"wp-block-heading\">I rebuilt my 944 Torque Tube<\/h4>\n\n\n\n<p>At Track Night I noticed a whirring noise when I was idling\non grid in neutral.&nbsp; The noise would go\naway if I mashed the clutch pedal.&nbsp; I had\nheard a similar noise on the back straight at Road Atlanta back in February, so\nI decided to check into it closer.<\/p>\n\n\n\n<p>With the car on the lift idling in neutral, there was\ndefinitely a noise coming from the middle of the torque tube.&nbsp; I decided it was time to change the bearings.<\/p>\n\n\n\n<p>I read through the procedure on <a href=\"http:\/\/www.clarks-garage.com\/shop-manual\/trans-05.htm\">Clarks Garage<\/a>. I also watched some Youtube videos. These looked intimidating, but I decided I had to give it a go.<\/p>\n\n\n\n<p>I began by removing the shifter from the rod and the torque tube.&nbsp; I then removed the transaxle.<\/p>\n\n\n\n<figure class=\"wp-block-image\"><img decoding=\"async\" loading=\"lazy\" width=\"1080\" height=\"608\" src=\"https:\/\/i2.wp.com\/mikestrawbridge.com\/blog\/wp-content\/uploads\/2019\/05\/torquetuberear.jpg?fit=525%2C295\" alt=\"\" class=\"wp-image-4963\" srcset=\"http:\/\/mikestrawbridge.com\/blog\/wp-content\/uploads\/2019\/05\/torquetuberear.jpg 1080w, http:\/\/mikestrawbridge.com\/blog\/wp-content\/uploads\/2019\/05\/torquetuberear-300x169.jpg 300w, http:\/\/mikestrawbridge.com\/blog\/wp-content\/uploads\/2019\/05\/torquetuberear-768x432.jpg 768w, http:\/\/mikestrawbridge.com\/blog\/wp-content\/uploads\/2019\/05\/torquetuberear-1024x576.jpg 1024w\" sizes=\"(max-width: 767px) 89vw, (max-width: 1000px) 54vw, (max-width: 1071px) 543px, 580px\" \/><\/figure>\n\n\n\n<!--more-->\n\n\n\n<p>I then removed the exhaust and the starter.&nbsp; Then I unbolted the tube from the clutch\ncover.<\/p>\n\n\n\n<figure class=\"wp-block-image\"><img decoding=\"async\" loading=\"lazy\" width=\"1080\" height=\"608\" src=\"https:\/\/i0.wp.com\/mikestrawbridge.com\/blog\/wp-content\/uploads\/2019\/05\/torquetubefront.jpg?fit=525%2C295\" alt=\"\" class=\"wp-image-4964\" srcset=\"http:\/\/mikestrawbridge.com\/blog\/wp-content\/uploads\/2019\/05\/torquetubefront.jpg 1080w, http:\/\/mikestrawbridge.com\/blog\/wp-content\/uploads\/2019\/05\/torquetubefront-300x169.jpg 300w, http:\/\/mikestrawbridge.com\/blog\/wp-content\/uploads\/2019\/05\/torquetubefront-768x432.jpg 768w, http:\/\/mikestrawbridge.com\/blog\/wp-content\/uploads\/2019\/05\/torquetubefront-1024x576.jpg 1024w\" sizes=\"(max-width: 767px) 89vw, (max-width: 1000px) 54vw, (max-width: 1071px) 543px, 580px\" \/><\/figure>\n\n\n\n<p>I recommend disconnecting the brake lines at this\npoint.&nbsp; I did it later and wished I had\ndone it earlier.&nbsp; I left the hand brake\ncables attached. <\/p>\n\n\n\n<p>I supported the axle tube on stands and removed the bolts as Clark\u2019s Garage suggests.&nbsp; I had to persuade the bushings to come loose from the body of the car using a large pry bar.&nbsp; I gently lowered the axle tube down about 4 inches.&nbsp; <\/p>\n\n\n\n<p>I then removed the three crossmember pieces that are under\nthe torque tube.&nbsp; I was then able to\nstart working the torque tube back toward the rear of the car.&nbsp; I was blocked by the heat shield for the\nmuffler and the fuel tank guard.&nbsp;\nHowever, I was able to flex the muffler heat shield enough to get the\nbell past it and then slide the torque tube the rest of the way out the rear of\nthe car.&nbsp; It was heavy and awkward, and I\nwished I had a helper, but I eventually got it out.<\/p>\n\n\n\n<figure class=\"wp-block-image\"><img decoding=\"async\" loading=\"lazy\" width=\"342\" height=\"608\" src=\"http:\/\/mikestrawbridge.com\/blog\/wp-content\/uploads\/2019\/05\/torquetubeout.jpg\" alt=\"\" class=\"wp-image-4966\" srcset=\"http:\/\/mikestrawbridge.com\/blog\/wp-content\/uploads\/2019\/05\/torquetubeout.jpg 342w, http:\/\/mikestrawbridge.com\/blog\/wp-content\/uploads\/2019\/05\/torquetubeout-169x300.jpg 169w\" sizes=\"(max-width: 342px) 100vw, 342px\" \/><\/figure>\n\n\n\n<p>With the tube out and on the floor, I measured the distance\nfrom the front of the tube to the tip of the shaft for reassembly\nreference.&nbsp; I used a soft faced dead blow\nhammer to tap the shaft into the tube.&nbsp;\nIt moved much more easily than I expected from watching videos.&nbsp; I found a piece of PVC pipe that fit over the\npilot nipple and was slightly smaller than the shaft diameter.&nbsp; I used that to drive the shaft the rest of\nthe way through the tube.&nbsp; <\/p>\n\n\n\n<figure class=\"wp-block-image\"><img decoding=\"async\" loading=\"lazy\" width=\"342\" height=\"608\" src=\"http:\/\/mikestrawbridge.com\/blog\/wp-content\/uploads\/2019\/05\/torquetubeshaftdriveout.jpg\" alt=\"\" class=\"wp-image-4965\" srcset=\"http:\/\/mikestrawbridge.com\/blog\/wp-content\/uploads\/2019\/05\/torquetubeshaftdriveout.jpg 342w, http:\/\/mikestrawbridge.com\/blog\/wp-content\/uploads\/2019\/05\/torquetubeshaftdriveout-169x300.jpg 169w\" sizes=\"(max-width: 342px) 100vw, 342px\" \/><\/figure>\n\n\n\n<p>I had a little trouble when the pipe slipped off the end of\nthe shaft somewhere past the second bearing.&nbsp;\nIt was difficult to get the pipe lined back up and on the end of the\nshaft again as the plastic pipe had a slight curve to it.&nbsp; Once it was lined up properly, the shaft\ndrove out easily.<\/p>\n\n\n\n<p>To remove the bearings, I used the threaded rod method described by <a href=\"http:\/\/www.clarks-garage.com\/shop-manual\/trans-05.htm\">Clark\u2019s Garage.<\/a>&nbsp; I used 9\/16 thread rod instead of \u00bd inch as I saw some people had trouble with the threads stripping. I got the threaded rod at Lowes.&nbsp; I used a Mazda crank bolt socket on the end of the rod to put force on the outer race of the bearings. I used two washers between the socket and the double nuts on that end.<\/p>\n\n\n\n<figure class=\"wp-block-image\"><img decoding=\"async\" loading=\"lazy\" width=\"1080\" height=\"608\" src=\"https:\/\/i0.wp.com\/mikestrawbridge.com\/blog\/wp-content\/uploads\/2019\/05\/TTbrearingsout.jpg?fit=525%2C295\" alt=\"\" class=\"wp-image-4967\" srcset=\"http:\/\/mikestrawbridge.com\/blog\/wp-content\/uploads\/2019\/05\/TTbrearingsout.jpg 1080w, http:\/\/mikestrawbridge.com\/blog\/wp-content\/uploads\/2019\/05\/TTbrearingsout-300x169.jpg 300w, http:\/\/mikestrawbridge.com\/blog\/wp-content\/uploads\/2019\/05\/TTbrearingsout-768x432.jpg 768w, http:\/\/mikestrawbridge.com\/blog\/wp-content\/uploads\/2019\/05\/TTbrearingsout-1024x576.jpg 1024w\" sizes=\"(max-width: 767px) 89vw, (max-width: 1000px) 54vw, (max-width: 1071px) 543px, 580px\" \/><\/figure>\n\n\n\n<p>On the flange end, I used an old Jeep Idler pully when Clark\nused a go cart pulley.&nbsp; I used my impact\nwrench to spin the rod and the bearings pulled out relatively easily.&nbsp; It got progressively harder to spin the rod\nas more bearings were picked up.<\/p>\n\n\n\n<p>When the bearing stack hit the idler pully, I could not pull and more.&nbsp; Rather than disassemble the puller, I simply loosened it a bit and used it like a slide hammer to pull the bearings the last bit out.<\/p>\n\n\n\n<p>I ordered bearings from Amazon.   <a href=\"https:\/\/amzn.to\/2QqvAqC\">6006 30x55x13mm 2Z ZZ Metal Shielded FAG Radial Deep Groove Ball Bearing<\/a><\/p>\n\n\n\n<p>My rearing were in the two piece holder that is riveted together.<\/p>\n\n\n\n<figure class=\"wp-block-image\"><a href=\"https:\/\/amzn.to\/2QqvAqC\"><img decoding=\"async\" loading=\"lazy\" width=\"1080\" height=\"608\" src=\"https:\/\/i2.wp.com\/mikestrawbridge.com\/blog\/wp-content\/uploads\/2019\/05\/ttbearings.jpg?fit=525%2C295\" alt=\"\" class=\"wp-image-4968\" srcset=\"http:\/\/mikestrawbridge.com\/blog\/wp-content\/uploads\/2019\/05\/ttbearings.jpg 1080w, http:\/\/mikestrawbridge.com\/blog\/wp-content\/uploads\/2019\/05\/ttbearings-300x169.jpg 300w, http:\/\/mikestrawbridge.com\/blog\/wp-content\/uploads\/2019\/05\/ttbearings-768x432.jpg 768w, http:\/\/mikestrawbridge.com\/blog\/wp-content\/uploads\/2019\/05\/ttbearings-1024x576.jpg 1024w\" sizes=\"(max-width: 767px) 89vw, (max-width: 1000px) 54vw, (max-width: 1071px) 543px, 580px\" \/><\/a><\/figure>\n\n\n\n<figure class=\"wp-block-image\"><img decoding=\"async\" loading=\"lazy\" width=\"342\" height=\"608\" src=\"http:\/\/mikestrawbridge.com\/blog\/wp-content\/uploads\/2019\/05\/ttoldbearing.jpg\" alt=\"\" class=\"wp-image-4969\" srcset=\"http:\/\/mikestrawbridge.com\/blog\/wp-content\/uploads\/2019\/05\/ttoldbearing.jpg 342w, http:\/\/mikestrawbridge.com\/blog\/wp-content\/uploads\/2019\/05\/ttoldbearing-169x300.jpg 169w\" sizes=\"(max-width: 342px) 100vw, 342px\" \/><\/figure>\n\n\n\n<p>I used a socket and my arbor press to press out the center ring.<\/p>\n\n\n\n<figure class=\"wp-block-image\"><img decoding=\"async\" loading=\"lazy\" width=\"342\" height=\"608\" src=\"http:\/\/mikestrawbridge.com\/blog\/wp-content\/uploads\/2019\/05\/ttbearingcenterpress.jpg\" alt=\"\" class=\"wp-image-4970\" srcset=\"http:\/\/mikestrawbridge.com\/blog\/wp-content\/uploads\/2019\/05\/ttbearingcenterpress.jpg 342w, http:\/\/mikestrawbridge.com\/blog\/wp-content\/uploads\/2019\/05\/ttbearingcenterpress-169x300.jpg 169w\" sizes=\"(max-width: 342px) 100vw, 342px\" \/><\/figure>\n\n\n\n<p>I then drilled out eh rivets holding the two halves together.  The halves were still held together by the rubber tire on the outside and the bearing in the middle.  I put the assembly in the vise with a socket supporting the bearing. I then used a pry bar to tap the halves apart.<\/p>\n\n\n\n<figure class=\"wp-block-image\"><img decoding=\"async\" loading=\"lazy\" width=\"1080\" height=\"608\" src=\"https:\/\/i0.wp.com\/mikestrawbridge.com\/blog\/wp-content\/uploads\/2019\/05\/ttbearingseperation.jpg?fit=525%2C295\" alt=\"\" class=\"wp-image-4971\" srcset=\"http:\/\/mikestrawbridge.com\/blog\/wp-content\/uploads\/2019\/05\/ttbearingseperation.jpg 1080w, http:\/\/mikestrawbridge.com\/blog\/wp-content\/uploads\/2019\/05\/ttbearingseperation-300x169.jpg 300w, http:\/\/mikestrawbridge.com\/blog\/wp-content\/uploads\/2019\/05\/ttbearingseperation-768x432.jpg 768w, http:\/\/mikestrawbridge.com\/blog\/wp-content\/uploads\/2019\/05\/ttbearingseperation-1024x576.jpg 1024w\" sizes=\"(max-width: 767px) 89vw, (max-width: 1000px) 54vw, (max-width: 1071px) 543px, 580px\" \/><\/figure>\n\n\n\n<figure class=\"wp-block-image\"><img decoding=\"async\" loading=\"lazy\" width=\"1080\" height=\"608\" src=\"https:\/\/i1.wp.com\/mikestrawbridge.com\/blog\/wp-content\/uploads\/2019\/05\/ttbearingseperation2.jpg?fit=525%2C295\" alt=\"\" class=\"wp-image-4972\" srcset=\"http:\/\/mikestrawbridge.com\/blog\/wp-content\/uploads\/2019\/05\/ttbearingseperation2.jpg 1080w, http:\/\/mikestrawbridge.com\/blog\/wp-content\/uploads\/2019\/05\/ttbearingseperation2-300x169.jpg 300w, http:\/\/mikestrawbridge.com\/blog\/wp-content\/uploads\/2019\/05\/ttbearingseperation2-768x432.jpg 768w, http:\/\/mikestrawbridge.com\/blog\/wp-content\/uploads\/2019\/05\/ttbearingseperation2-1024x576.jpg 1024w\" sizes=\"(max-width: 767px) 89vw, (max-width: 1000px) 54vw, (max-width: 1071px) 543px, 580px\" \/><\/figure>\n\n\n\n<figure class=\"wp-block-image\"><img decoding=\"async\" loading=\"lazy\" width=\"342\" height=\"608\" src=\"http:\/\/mikestrawbridge.com\/blog\/wp-content\/uploads\/2019\/05\/ttbearingapart.jpg\" alt=\"\" class=\"wp-image-4973\" srcset=\"http:\/\/mikestrawbridge.com\/blog\/wp-content\/uploads\/2019\/05\/ttbearingapart.jpg 342w, http:\/\/mikestrawbridge.com\/blog\/wp-content\/uploads\/2019\/05\/ttbearingapart-169x300.jpg 169w\" sizes=\"(max-width: 342px) 100vw, 342px\" \/><\/figure>\n\n\n\n<p>I fit a new bearing in one half. I then slipped the tire on.  I used a drill bit to line up the holes so new rivets would fit. I then used the vise to press the parts together.<\/p>\n\n\n\n<figure class=\"wp-block-image\"><img decoding=\"async\" loading=\"lazy\" width=\"1080\" height=\"608\" src=\"https:\/\/i0.wp.com\/mikestrawbridge.com\/blog\/wp-content\/uploads\/2019\/05\/ttbearingreassembly.jpg?fit=525%2C295\" alt=\"\" class=\"wp-image-4974\" srcset=\"http:\/\/mikestrawbridge.com\/blog\/wp-content\/uploads\/2019\/05\/ttbearingreassembly.jpg 1080w, http:\/\/mikestrawbridge.com\/blog\/wp-content\/uploads\/2019\/05\/ttbearingreassembly-300x169.jpg 300w, http:\/\/mikestrawbridge.com\/blog\/wp-content\/uploads\/2019\/05\/ttbearingreassembly-768x432.jpg 768w, http:\/\/mikestrawbridge.com\/blog\/wp-content\/uploads\/2019\/05\/ttbearingreassembly-1024x576.jpg 1024w\" sizes=\"(max-width: 767px) 89vw, (max-width: 1000px) 54vw, (max-width: 1071px) 543px, 580px\" \/><\/figure>\n\n\n\n<p>I then used a grinder to cut one side of the flat off the rivet so it would sit flush against the edge of the housing.  I then used three rivets to hold the halves together.   I then used the arbor press again to reinstall the center rings.<\/p>\n\n\n\n<p>To press the new bearings in, I lubricated the tires with tire mounting lubricant. I&#8217;m sure dawn would work as well.  I used the following diagram for where to place the new bearings in the tube.<\/p>\n\n\n\n<figure class=\"wp-block-image\"><img decoding=\"async\" loading=\"lazy\" width=\"1080\" height=\"608\" src=\"https:\/\/i1.wp.com\/mikestrawbridge.com\/blog\/wp-content\/uploads\/2019\/05\/ttbearing-spacing.jpg?fit=525%2C295\" alt=\"\" class=\"wp-image-4975\" srcset=\"http:\/\/mikestrawbridge.com\/blog\/wp-content\/uploads\/2019\/05\/ttbearing-spacing.jpg 1080w, http:\/\/mikestrawbridge.com\/blog\/wp-content\/uploads\/2019\/05\/ttbearing-spacing-300x169.jpg 300w, http:\/\/mikestrawbridge.com\/blog\/wp-content\/uploads\/2019\/05\/ttbearing-spacing-768x432.jpg 768w, http:\/\/mikestrawbridge.com\/blog\/wp-content\/uploads\/2019\/05\/ttbearing-spacing-1024x576.jpg 1024w\" sizes=\"(max-width: 767px) 89vw, (max-width: 1000px) 54vw, (max-width: 1071px) 543px, 580px\" \/><\/figure>\n\n\n\n<p>I used the sane threaded rod set up I used to extract the bearings.  I pressed the them from their near end so I did not have to move them so far down the tube.<\/p>\n\n\n\n<p>I then stood the tube on the bell housing and lowered the shaft into place.  I coated the shaft with rubber lubricant as well.  I used a dead blow hammer to keep it moving. I set the splined section to the same stick out as I had before disassembly.<\/p>\n\n\n\n<p>I enlisted some help to get the torque tube back in the car.  I slid it in place and aligned the splines into the clutch disk.   I then raised the rear suspension back into position and reattached the three crossmembers. <\/p>\n\n\n\n<p>I then reinstalled the transaxle, exhaust and other parts I had removed.  No more whirring in neutral.<\/p>\n\n\n\n<figure class=\"wp-block-image\"><img decoding=\"async\" loading=\"lazy\" width=\"342\" height=\"608\" src=\"http:\/\/mikestrawbridge.com\/blog\/wp-content\/uploads\/2019\/05\/torquetubedone.jpg\" alt=\"\" class=\"wp-image-4976\" srcset=\"http:\/\/mikestrawbridge.com\/blog\/wp-content\/uploads\/2019\/05\/torquetubedone.jpg 342w, http:\/\/mikestrawbridge.com\/blog\/wp-content\/uploads\/2019\/05\/torquetubedone-169x300.jpg 169w\" sizes=\"(max-width: 342px) 100vw, 342px\" \/><\/figure>\n","protected":false},"excerpt":{"rendered":"<p>I rebuilt my 944 Torque Tube At Track Night I noticed a whirring noise when I was idling on grid in neutral.&nbsp; The noise would go away if I mashed the clutch pedal.&nbsp; I had heard a similar noise on the back straight at Road Atlanta back in February, so I decided to check into &hellip; <\/p>\n<p class=\"link-more\"><a href=\"http:\/\/mikestrawbridge.com\/blog\/2019\/05\/porsche-944-torque-tube-bearings\/\" class=\"more-link\">Continue reading<span class=\"screen-reader-text\"> &#8220;Porsche 944 Torque Tube Bearings&#8221;<\/span><\/a><\/p>\n","protected":false},"author":1,"featured_media":0,"comment_status":"closed","ping_status":"open","sticky":false,"template":"","format":"standard","meta":[],"categories":[1],"tags":[],"_links":{"self":[{"href":"http:\/\/mikestrawbridge.com\/blog\/wp-json\/wp\/v2\/posts\/4962"}],"collection":[{"href":"http:\/\/mikestrawbridge.com\/blog\/wp-json\/wp\/v2\/posts"}],"about":[{"href":"http:\/\/mikestrawbridge.com\/blog\/wp-json\/wp\/v2\/types\/post"}],"author":[{"embeddable":true,"href":"http:\/\/mikestrawbridge.com\/blog\/wp-json\/wp\/v2\/users\/1"}],"replies":[{"embeddable":true,"href":"http:\/\/mikestrawbridge.com\/blog\/wp-json\/wp\/v2\/comments?post=4962"}],"version-history":[{"count":4,"href":"http:\/\/mikestrawbridge.com\/blog\/wp-json\/wp\/v2\/posts\/4962\/revisions"}],"predecessor-version":[{"id":5005,"href":"http:\/\/mikestrawbridge.com\/blog\/wp-json\/wp\/v2\/posts\/4962\/revisions\/5005"}],"wp:attachment":[{"href":"http:\/\/mikestrawbridge.com\/blog\/wp-json\/wp\/v2\/media?parent=4962"}],"wp:term":[{"taxonomy":"category","embeddable":true,"href":"http:\/\/mikestrawbridge.com\/blog\/wp-json\/wp\/v2\/categories?post=4962"},{"taxonomy":"post_tag","embeddable":true,"href":"http:\/\/mikestrawbridge.com\/blog\/wp-json\/wp\/v2\/tags?post=4962"}],"curies":[{"name":"wp","href":"https:\/\/api.w.org\/{rel}","templated":true}]}}