How to save gas in your Jeep

How to save gas in your Jeep

Jeeps are known more for their utility than for their fuel economy. The fact that we add large tires and lift them often adds to their thirst for fuel. However, there are a few simple things that you can do to save gas in your Jeep.

The single largest factor in how much gas your Jeep uses is how it is driven. Making slow starts and driving at a steady speed will do more to save gas in your Jeep than any thing else you can do.

Large off road tires can add rolling resistance to your Jeep causing it to use more gas. Lower air pressure that makes them get more traction off road also causes them to be more resistant to rolling on pavement. Bringing tires back to full pressure when driving on the road will help save gas. Also, having a set of street tires can help save gas and reduce wear on your off road tires.

Having the right gear ratio will also keep your engine in the proper operating range for better fuel economy. As you go up in tire diameter, you also need to go up in gears to match. This will keep your engine operating in the proper RPM range for optimum efficiency.

Another simple way to save gas is to reduce the stuff you carry around. Stronger bumpers, skid plates and winches all add weight and require more fuel to carry around. Any extra gear that can be removed and stowed between trips can help save gas. So look at leaving the High Lift and other heavy items at home.

Low restriction air filter systems and low restriction exhaust can also help save gas. Replacing the stock manifold with a header can add a small amount of engine efficiency. The stock system is very efficient and only small improvements can be expected. However, if the exhaust system is damaged, it may be adding fuel wasting restrictions. Dirty air filters and damaged air intake plenums can also reduce economy.

External accessories such as roof racks and wider fender flares will add aerodynamic drag to your Jeep. Keeping the exterior sleek will help save gas.

A well lubricated vehicle will also have less drag and use less gas. Save gas by adding friction reducing oil additives to the engine at every oil change. Using a lighter weight oil can also help save gas. Check the owner’s manual for the proper weight of oil for your Jeep’s engine. I have had good results for adding Market America’s Friction Free 3000 to each oil change.

Keeping the engine’s ignition system in top shape will also help save gas. Fresh spark plugs and wires will ensure that every ignition cycle results in a complete burn. I use the Champion RC9YC plug gapped a bit wider than stock to increase gas mileage on my Jeeps. A high energy ignition system like a MSD or Jacobs will be helpful on older Jeeps but less improvement will be seen on modern engines that have high energy systems stock. When changing the plug wires, it is a good idea to change the distributor cap and rotor to complete the renewing of the electrical system.

There are a few sensors that can reduce fuel economy in the engine if they malfunction. The most important is the oxygen sensor. If this sensor is damaged or contaminated, the computer may not inject the proper mixture of fuel. Replacing the oxygen sensor at the specified intervals may help you save gas. I have also found that the engine temperature sensor needs to provide correct information to he computer for optimum fuel economy. If you have a Cherokee and the electric fan is not coming on as expected, this sensor may be at fault. Replacing it will also help you save gas.

Several fuel additives have been promoted as ways to save gas. I have tried adding acetone and other chemicals but I have not seen any improvement in economy. However, occasionally adding SeaFoam to the fuel seems to help keep the injectors clean and helps with engine drivability with in turn helps save gas. I have also seen some benefit to using Market America’s fuel enhancer. The MA fuel enhancer also helps keep the fuel level sending unit clean so that it correctly indicates the level in the tank. This sensor tends to pick up sulfates form the fuel causing it to not read correctly. The MA fuel enhancer seems to reduce this build up.

One last note on fuel, fuel with ethanol will increase fuel consumption. I have seen as much as 10% gas saving by using gasoline without ethanol added. In addition I have found that fuel with ethanol tends to cause the idle air control valve to stick. If possible, avoid fuel that has had ethanol added.

Water to Gas

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Rear Disk Brake Conversion – Jeep Cherokee

Rear Disk Brake conversion on a Jeep Cherokee

ZJ disk Brakes on an XJ

I converted the rear brakes on my Jeep Cherokee from drums to disks. I used parts from a 96 ZJ Dana 35 to make the conversion.

I removed the brake backing plates, hand brake cables, hydraulic lines, and mounting brackets from the ZJ axle. I also pulled the bracket that holds the cables to the body as well as the brake adjuster and balance bar. The conversion might have been easier if I had pulled the ZJ handbrake lever as well.

Removing the drum brakes from my XJ meant disassembling my Lock Rite locker to get the C clips loose. This is not a big job except that it never comes apart like I think it should and it takes me a while to remember which slot the C clip has to exit through.

When I pulled the cover, I noticed that it had been way too long since I changed the gear oil in the diff. I also noticed that on a previous outing where I had banged the diff cover on a stump, it had in fact made contact with the ring gear. The gear is fine but the cover had a cut in it. I hammered the cover back close to its original shape while I had it off.

With the axles out of the way, the drum brakes came off with four mounting bolts. My backing plates were stuck to the axle with dirt and rust and had to be tapped with a hammer to slide them off the end of the axle housing.

I found that the center hole in the disk brake plate was too small to go over my 8.25 housing. I used a milling bit chucked in my drill press to enlarge the hole so it would slide over. The bolt pattern matched. The mounting studs on the 8.25 are a little too short but there seems to be enough thread engagement. If I ever do this swap again, I will pull the mounting studs from the ZJ axle as well.

With the backing plates mounted, I attached the calipers to the plates. The upper bolt is partially obstructed by the leaf spring, but it went in anyway. I also found that if the bolt is slipped into the caliper before it is set in place it all goes together easily.

I used the hydraulic lines from the ZJ. The line on the left brake was close to the right shape and required only minor bending. The long line to the right brake required quite a bit of re shaping to go over the 8.25 pumpkin and line up with the caliper. It eventually fit. The rubber line from the axle to the body matched up perfectly with the XJ hard line at the body. There is also the advantage that the ZJ line is longer than the XJ line so I don’t have the line limiting the droop as before.

ZJ disks on a XJ 8.25

I used the ZJ hand brake cables because the XJ cables have a different end on them. I removed the bracket from the bottom of the ZJ and cut it in half. I used only the rear half. I bolted the rear half to the floor of my XJ just above where the old cable clips are.

Hand Brake cables using ZJ bracket

I used the balance bar from the ZJ and used the ZJ brake adjuster rod as an extension on the XJ brake rod. I had to add a couple more inches to the rod to make it all connect up.

ZJ hand brake cable bracket

Once diff was refilled with gear oil and the brakes bled I mounted the wheels. One thing I had over looked was that the rotors are enough thicker than the drums to make the lugs bolts too short. I will have to replace these as they need another thread or two to be fully engaged with the lug nuts. If I had closed end nuts I would never have noticed.

Stopping power is vastly improved over what I had because I had a leaking wheel cylinder on the drum brakes. I used the original proportioning valve.

It took several adjustments to get the hand brake tight enough to hold on my steep driveway. However, once the slack was out of the cables, it held fine. My hand brake has not worked right on the drums for a couple of years so it will be really nice to not have to find trees to brace against when I need to hop out on the trail.

Electric Fan Override Switch Jeep Cherokee

On the last couple of off road outings, I have had some trouble with my Jeep Cherokee overheating. Normally this Jeep has performed well with respect to heat so this was a surprise to me.

For some reason, the coolant temperature switch was not bringing in the electric fan. Also, since I have disconnected the AC, I could not force it on by turning on the AC compressor.

To get me through the day of wheeling, I ran a wire from the battery to the fan so that it ran all the time. While this kept me cool, it was inconvenient to have to open the hood and disconnect the wire every time I stopped for any length of time.

Back at home, I wired up the jumper through a switch on the dash so I could easily control the fan. I connected the hot side directly to the positive battery terminal and the other side I spliced into the red wire going to the fan.

Splice into the fan wire

New switch on the dash for the fan

This switch will cause the fan to run even with the engine off. It also bypasses all the relays and other parts of the circuit that might give trouble. The drawback is that the full fan current has to go through the switch.

In order to have a more convenient way to power up the fan when before the temp switch kicks in, I also modified the AC control circuit. This circuit also brings in the fan when the compressor clutch is engaged. Since my AC is long gone, but the compressor is still there, I unplugged the clutch power and put a jumper in the low freon switch. So if I switch on the AC, the radiator fan will run. This way, I can have the fan switch on and off with the engine.

Low freon switch jumper and AC compressor unplugged

Pinion Alignment with Axle Shims on a Jeep Cherokee

Pinion Alignment with Axle Shims on a Jeep Cherokee

When lifting a Jeep Cherokee, the pinion angle changes relative to the transfer case. The alignment must be within the limits of the universal joints to prevent driveline vibrations.

One method of adjusting the pinion angle is to use angled shims. These shims are placed between the spring and the spring perch to rotate the pinion to match the drive shaft.

When a Jeep is lifted three inches or more, the drive shaft angle exceeds the recommended limits for the universal joints. A common method to correct the alignment while retaining the stock drive shaft is to drop the transfer case one inch and use two degree shims or use angled lift blocks like the Rough Country Lift kit includes.

In order to eliminate the misalignment, a Slip Yoke Eliminator kit is often used on the rear of the transfer case. Several versions are available for the NP231 that replace the output shaft with a stronger, shorter shaft giving multiple advantages for one simple modification.

With a Slip Yoke Eliminator kit installed, the standard drive shaft is replaced with a double cardon type like the one used in the front of the Cherokee. In fact, if you have an automatic transmission, a stock front shaft can be used in the rear with a SYE conversion.

The double cardon type shaft however uses a very different alignment from the standard shaft. Quite a bit of axle rotation is needed to align the pinion.

In the standard configuration, the pinion and the transfer case are aligned to be parallel to each other. The idea is to have the same operating angle for both universal joints on the drive shaft.

The double cardon shaft uses a special joint with two universal joints at one end and a singe joint at the other end. The correct alignment is to have the drive shaft parallel to the pinion and the entire angle is made up in the two joints on the opposite end.

For a three inch lift, I found about 8 degrees of shim was needed. This Jeep was fitted with two degree blocks so adding six degrees of angle to the spring pack brought it into alignment.

To calculate the shims needed, you will have to use trigonometry. However it is not too bad using this simple method.

With the transfer case and axle in place, I mounted the drive shaft. The misalignment was immediately evident. I placed a straight edge along the bottom of the pinion and parallel to the pinion shaft. I then measured the distance from the drive shaft center to the top of the straight edge. In my case, I measured to a point 30 inches up the shaft and found it need to be raised three inches to make it line up.

Now divide the distance it is off by the distance up the shaft. In my case it was 3 divided by 30 or 0.1.

To convert this number to the angle, you need to take the arctangent of the number. This is easily done on a scientific calculator or even easier to do using Google. In my case I typed arctan(3/30) in degrees into the Google search line. Google returns this result: arctan(3 / 30) = 5.71059314 degrees. Round it to the nearest degree and try that shim. In my case a six degree shim was really close and worked fine.

To install the shim, you have two options. If you get a steel shim, you can weld it to the spring perch making it a permanent part of the axle. I chose to add it to the spring pack so that it can be easily changed if I want to add longer shackles or different lift blocks.

To install the shim in the spring pack, you will have to disassemble the spring pack. It is generally a good idea to replace the center pin and the shim kit came with new center pins. So you can just cut off the nuts from the center pins. They are often impossible to unbolt due to dirt and corrosion.

Begin by removing the U bolts that hold the axle to the spring. Separate the spring from the perch. Next, use two large C clamps to hold the spring pack together while you remove the center bolt.

Place the new bolt through the shim and then pass the bolt through the spring pack. Tighten the nut. Be sure the fat end of the shim is to the rear to rotate the pinion up for the Cherokee. Align the pin with the block or spring perch and press it back together with a floor jack under the axle. Cut off the excess bolt length on the center pin.

Reinstall the U bolts and tighten them to the proper torque. Give it a good whack with a hammer to make sure every thing seated right and recheck the torque. It is good to recheck the U bolts after the first run as they sometimes move around on the axle tube and loosen up.

Verify the alignment visually or with a straight edge. If it looks right, congratulations! Put the wheels back on and give it a test drive.

Rough Country Suspension Suspension Lift Kit

Golden Mountain Off Road Park – Labor Day

Golden Mountain Off Road Park.

We celebrated Labor Day and Princess’s birthday by going off roading at Golden Mountain Off Road Park. I spent the early part of the weekend installing Princess’s SYE equipped 231 Transfer case and getting the pinion angle right in the rear. But by Monday, we were ready to hit the trails.

Our previous visits to Golden Mountain had been last fall when the trails were wet and slippery. This trip they were dry and dusty.

At the park entrance we were greeted by the very friendly park owners. They made us feel very welcome.

After unloading my truck from the trailer and removing the doors from both Cherokees, we headed up trail one. Trail one has always been our nemesis in the wet. It is marked easy on the map but even in dry conditions it is challenging. On our previous attempts is has proven impassable.

This time we made it all the way to the top. Coming back down the other side of trail one proved to be even more of a challenge however. This part of the trail has eroded into a deep V notch right down the center of the trail. The only real way down is to straddle the V. I made it fine but Jenny got hung up in one of the transitions. I had to help her get untangled.

Once down from there, we headed up trail 11. This is a fun rocky climb. There was a spot where Jenny got hung last time, but this time equipped with lockers, a SYE and no doors, she made it easily.

At the top of 11 we made our way to 12 and made the loop. Trail 12 has several rocky sections and then ends in a long hill climb. Jenny got hung in a muddy spot last trip, but there was no mud to hang in this time. Just lots of dust. The dust made some of the climbs slippery, but not like the mud.

We took trail 29 down to intersect with trail two and took a break. This was our first time on 29 with was pretty easy in the dry but would be very slippery if wet.

After a rest break we headed up trail two to Jenny’s favorite ledges. Again they were much easier in the dry.

At the top, we toured the pavilion and the camping areas. Here I noticed my Jeep was running very hot. I soon discovered that the electric fan was not working.

We made the short trip down the paved road to the trailer and I scavenged wire from Jenny’s Jeep to make a jumper for the fan. I simply wired it directly to the battery so that meant every time I stopped for any length of time, I had to open the hood and disconnect the wire.

We headed back up the trail and made the 12, 29, 2 loop again. This time we decided to try an unmapped spur off trail 11. This brought us out at one of the pavilions across from the lake. My Jeep was still running hot so I let it cool and added some water.

Scott called and we arranged to meet him at the gate. After picking him up, we ran back up trial one again. This time we took trail 10 on our way to see the top of bounty hill. Trail 10 we found has a very scary section where you have to make two very steep drops in about the length of the Jeep. Scott spotted me down and then did the same for Jenny. I was really glad we did not have to go back up that section.

The climb back out of the hole was still pretty challenging as it is a steep rutted climb. The climb ends with a choice of two big boulders that you have to climb the face of. I did not want to loose momentum, so I made a quick decision of the one on the left. That turned out to be a good choice and I made it up easily. I got out and was able to spot Jenny to the smaller boulder as well.

My Jeep was running much better with the fan on and the radiator full of water. I was really glad that I was able to make a simple fix.

We took time to climb on the boulders overlooking bounty hill. I have watched videos of buggies going up it but I would really like to see one in person.

Next we went down trail 27 to one and made our way to 21. This required running the same part of one that gave us trouble earlier in the day. Jenny got hung up in the same spot again. With Scott spotting me I drove her Jeep up onto the bank and out over the V notch. At one point Scott said the front tire was about two feet in the air but it did not feel tippy until it had already started back down.

We drove up 21 and took a look at Hellivator and some of the other climbs in the same area. We all agreed that we look forward to watching someone do these climbs.

We turned around and headed back down trail 21. We took 11 for the third time just because it is fun and took the exit by the small pavilion. We stopped again to tour the big pavilion and take advantage of the facilities there. Caleb enjoyed the playground for a while too.

We headed back into the trail 12 loop and then took 29 back down and then exited on the lower part of trail 2. By the time we made it back to the trailer, we were all very tired and dusty, but we really enjoyed our day at Golden Mountain.