Archive for the ‘Safety’ Category

Second Prototype Gas Tank Skid Plate

Tuesday, January 10th, 2012

Second Prototype Gas Tank Skid Plate

I liked the skid plate I fabricated for Jennifer’s XJ so well that I decided to make one for my Jeep. I did however make a few changes in the design. I did not like the way I bolted hers in place by tapping into the thin metal frame rails. One of the bolts stripped out and had to be replaced with another one near by. I have bought rivet nuts to strengthen it next time it is taken off her Jeep.

For mine, I decided to fabricate a bolt strip to insert inside the frame rail. To make the strip, I first had to remove the rear bumper. This is easy on my off road Jeep due to the way the custom pipe bumper is made. I also took this opportunity to remove two broken off bolts in the bumper mounting surface.

The first one was accessible from behind the bolt hole so I simply clamped vise grips onto the end of the bolt and turned it out the back. I did have to use some heat and penetrating oil to get it to turn but one it did, it came right out the back.

The second bolt was at the top and I could not access it with vise grips. I could however spray penetrating oil on the exposed part. I first tried cutting a slot in the bolt and turning it with a screw driver. That did not work at all. Next I made a deeper slot and tried my impact driver. I was able to turn the bolt about half a turn before it stopped again. Even heating it cherry red did not help.

Next I took a nut and welded it to the broken off bolt. I used my flux core wire welder to make the weld. The bolt came out relatively easily with the nut welded to the top.

I measured for the two holes that were already in the frame rails. I then marked an approximate location for the third bolt. I drilled the holes in the angle used for the mounting bracket. I then made a strip of flat bar with the same hole spacing using angle as a jig. I then welded in two bolts into the holes that lined up with the two in the frame rail. I used a magnet to slide the strip into place and temporarily bolted the angle in place. I then drilled through the hole in the bracket into the frame rail. I then removed both parts and welded in the third bolt.

I repeated the procedure for the other side. I had to open the hole at the rear of the Jeep slightly to get the strip inside. I used a cut off wheel to make two vertical slits and then bent the metal out to open the hole enough to get the bolt strip in. Fishing it under the gas filler section was challenging but it worked.

With the mounting points fabricated, I used the template from the first skid plate to lay out the side pates. I extended them about a quarter of an inch to give a little extra clearance when installing the plate. The bottom plate ended up about a half inch wider. I am not sure how that happened. However, I like the extra clearance on the side of the tank.

Another change I decided to make was the exhaust hanger. Jennifer’s uses the exhaust hanger bolts as mounting bolts. However, these proved extremely difficult to install when mounting the skid plate. For mine I fabricated studs and welded them to the mounting angle. Now I can simply slip the hanger over the studs and install two nuts. I expect this to be much easier.

I currently have the sides and the bottom tack welded together. My next step is to remove the assembly from the Jeep and complete the welds. I picked up a new roll of wire for the welder today.

UPDATE: Last night I took it down and did the final welding. I finished off the spool of wire that came on my MIG so I had to learn how to change wire in the middle of the welding process. I ground down the edge and now it is ready to be sanded for paint.

Skid plate bolts

frame holes opened up

mounting bolts for skid plate

studs for the exhaust hanger

finished gas tank skid plate

UPDATE 2: I added a small lip at the front edge that adds a lot of strength to the plate. I also sanded it down and painted it black.

Exhaust hanger detail

Exhaust in place

Filler cover detail

Jeep Cherokee Power Steering Hose Replacement

Tuesday, January 3rd, 2012

Jeep Cherokee Power Steering Hose Replacement

I have replaced several power steering hoses on various Jeep Cherokees. It has gotten to be a pretty straight forward job. See this previous post on how to replace a power steering hose.

Janice’s 1999 Cherokee had been emitting a puff of smoke each time she turned her XJ to full lock. Although there was little sign of a leak on the hose, our experience with the Green Jeep catching fire due to a power steering hose leak made me extra cautious.

I got a new hose and then pulled the electric fan and the air box to make room. I tried using the various 18mm wrenches I had to get the hose loose from the steering box. I have always been successful in the past using an open end wrench. However, this one refused to budge.

I picked up a set of crow foot flare nut wrenches from my local NAPA store. They have a great set of tools in a nice case for around $20. Unfortunately I forgot that the bottom is an 18mm and the top is a 5/8 inch. I bought only the SAE set. The store was closed for the holiday by the time I figured out I also need the metric set.

Jennifer rescued me by searching until she found a set at O’Reilly’s. It is still a nice set for about the same price as the NAPA set but does not have the nice case.

I used the 18 metric crow foot flare nut wrench to break loose the lower line. It took a lot of torque but it eventually broke free. Janice and Jennifer were able to finish taking it out using the 18mm stubby wrench.

I used the 5/8 crow foot to pop loose the upper hose. It was not nearly as tight. I showed them how to put on the O rings on each end of the hose and let them get the lines threaded into place. The lower one always seems to be difficult and takes some patience to get it started.

After the new line was installed, I had them add some fluid and jack up the front of the Jeep. They turned the wheel from lock to lock to bleed the air out of the line. After that, they started the engine and repeated the process.

Once most of the air was out, she turned the wheel to one of the locks and listened for the pressure relief to open. There was a noticeable change in sound as the last of the air purged.

I rechecked the level of fluid in the power steering reservoir and checked for leaks again. Now we all feel much safer driving the Jeep.


Powercraft Power Steering Pressure Hose – 80290

Powercraft Power Steering Pressure Hose - 80290

How to Replace Rear Brake Shoes on a Jeep Cherokee

Tuesday, December 27th, 2011

How to Replace Rear Brake Shoes on a Jeep Cherokee

While many people swap in disk brakes, the rear drum brakes on the Jeep Cherokee work pretty well when they work correctly. They self adjust each time they are applied in reverse. The shoes will generally last at least 100,000 miles.

Begin by lifting the Jeep and removing the rear wheel. Next remove the brake drum. If it has never been off before, there will be one or two spring clips on the lug studs. Grab these with pliers and break them away or try to unscrew them from the studs.

Pull on the drum to remove it. If it hangs on the shoes, remove the rubber cap on the backing plate and use a brake spoon to release some of the tension on the shoes. Rotate the adjuster up to release.

If the drum hangs on the hub, try hitting the face of the drum with a hammer. This will often break loose the rust weld at the center. Penetrating oil may help as well. In severe cases you may need a drum removal tool.

Once the drum is removed, inspect the brakes. There should be two overlapping springs at the top, an adjuster cable running from the top to the bottom of the rear shoe, retaining springs on each shoe and a smaller spring connecting the two shoes at the bottom.

The adjusted lever should lightly contact the wheel on the adjuster screw. The screw should turn freely when the adjuster lever is moved away from it.

If any of the springs as broken or missing, you will need a spring kit with the new shoes. If the cable or the adjuster is not working properly, you will also need a small parts kit.

To remove the shoes, I start with the retaining clips. Press in on the cup using either a brake tool or a pair of vise grips. Reach behind the backing plate and rotate the pin until it lines up with the slot in the cup. Release the spring to separate it from the pin. Use the same procedure on the other shoe.

Next remove the two large springs at the top. Use either a spring tool or a pair of vise grips to release one spring at a time. Note that the spring on the rear shoe also holds the cable pivot in place. Note the arrangement so you can put it back later.

The two shoes can now be slipped down around the axle and the lower spring can be removed as well as the adjuster. Pay attention to how the hand brake lever engages the rear shoe so you can put that back later. Also note the orientation of the adjuster screw. I like to lay all the parts out on the floor in a sort of exploded view so that I can reference it upon reassembly.

The mounting pin for the new shoes will likely not be installed. To put it in, note which side it is mounted on the old shoe. Use a vise to press the pin into the hole in the new shoe.

Put a small dab of grease on the backing plate in the places where the shoes contact. Also inspect the wheel cylinder and replace it as necessary before installing the new shoes.

Set a shoe in place and set the retaining spring over the hole. Insert the pin from the rear and align it with the slot in the cup. Compress the spring and rotate the pin to lock into the cup. Then release the spring to hold it in place. Do the same with other shoe. Note that the front and rear shoes are different. Make sure you have them in the correct place. Also make sure they properly engage the wheel cylinder. Slip the bar in place between the shoes in the upper slots.

Put the loop of the cable over the anchor pin. Hook the spring for the front shoe in the hole and use a spring tool to hook the spring over the anchor pin. Carefully place the cable pivot into the hole in the rear shoe. Hook the spring to hold it in place. Use the tool to secure the spring to the anchor. Inspect the pivot to make sure it is properly engage in the hole and is flat against the shoe. Adjust as needed.

Use pliers to install the lower spring between the shoes. Rotate the adjuster screw to fully closed. Stretch the spring and slip the adjuster screw in place between the screws. Clip the adjuster lever to the pin in the rear shoe. Install the spring on the lever. Tip the lever up and attach the adjuster cable making sure it is routed properly around the pivot.

When properly fitted, the lever will be against the cog wheel o the screw. It if hangs above or below the wheel, adjust the pivot under the spring. Adjust the screw until the drum will go on with just a slight drag. Install the drum and make a final adjustment of the screw through the access hole in the backing plate.

Repeat the procedure on the opposite side. Keep in mind however that the other side is reversed and even the screw threads on the adjuster screw are opposite.

Saving on Propane costs

Saturday, December 10th, 2011

Saving on Propane costs

I recently noticed that our propane costs have gone up a huge amount. I know the cost of propane has increased, but our usage is up as well. We use propane only for the stove and the water heater so we really should not use very much propane at all. In fact over the 15 plus years we have lived in this house I have pretty much ignored the propane bills and just let the truck driver stay on top of keeping my tank filled.

However I am paying the price for my inattention right now.

I started by setting back the thermostat on the hot water heater. There is no use heating the utility room any more than necessary. The clothes dryer does a good enough job with that.

Next I started checking for leaks. I mixed up a batch of soap and water and put it in spray bottle. I went around outside spraying joints. I started at the tank and worked my way back to the house. I checked the regulator vent as well because a broken diaphragm could be a big leak.

I finally found a joint that bubbled where the line entered the house for the stove. It had been repaired a few years ago and one of the fittings made a few bubbles. Snugging up the nut made the bubbles quit.

Next I checked around the hot water heater. It was relocated a couple of years ago when the floor was redone. Sure enough there was a leak where the copper pipe joined the shut off valve. I had to tighten the nut twice to get it to completely stop.

I had thought the smell around the hot water heater was just the kitty litter box but I guess it was the mercaptane in the propane after all. A couple of hours after I tightened the fitting, the air was much fresher smelling in the laundry room. I hope this will also translate in to lower propane bills as well.

Leaf Spring Repair on the Trail

Tuesday, November 8th, 2011

Leaf Spring Repair on the Trail

This past weekend in Harlan, Ky our group experienced two serious leaf spring failures. In my case I was able to get my jeep back to camp make repairs there. In the second case, we had to repair the Jeep before it could be extracted from the obstacle where it broke.

On my Jeep, I noticed that the rear axle was moving back under braking. It would sometimes contact the rear of the fender opening. I carefully drove I back to camp minimizing the scraping on the tire.

Once I removed the wheel, I saw that the center pin of the spring pack had sheared off. This loss allowed the axle to move the rest of the spring pack along then main leaf.

I used a floor jack under the axle to support it. I then used a Hi Lift jack to lift the body of the XJ enough to unload the spring. I sat the Jeep down of a large log to give it stability during the repair.

After removing the U bolts, I was able to line up all the leafs of the spring pack and drive out the remainder of the pin. I then went into town and was able to buy a new set of pins at Advance Auto.

I used a screwdriver to line up the holes in the leaves and slipped the new pin into place. I used two C clamps to compress the spring pack while I tightened the pin. Once the spring pack was back together, I used a ratchet strap to pull the axle back into alignment with the spring pack. I then used the floor jack to press the pin into the hole in the axle.

I then reinstalled the U bolts and tightened then securely. I remounted the wheel and removed the blocks. I will inspect the other side and replace that pin in my shop at home.

The second leaf spring failure of the weekend was more serious. At the end of an especially difficult obstacle, my friend broke the main leak spring just in front of the axle tube. This breakage allowed the axle to move forward and back uncontrolled as well as side to side some. He was unable to move more than a few feet at a time.

His Jeep was also in a precarious place. We were able to get the spring back into place enough for him to roll back down to a somewhat level spot. We then used the weight of the Jeep to force the two parts of the spring close to the correct position.

Next we used two C clamps to press the main leaf into the supporting leaves. Friction between the leaves held it together. He added several wraps of baling wire to give some lateral support. He then added a ratchet strap to keep the whole assemble from sliding apart to the rear.

Which the spring secured in this manner, he was able have his XJ winched out of the hole it was in and then he was able to drive it a few miles down the trail to where we could pick it up on his trailer.

Through some clever thinking and working together, both of us were able to keep our Jeeps going. By working with the tools and supplies available both Jeeps made it home safely and without an expensive tow bill.