1G DSM headliner repair

1G DSM headliner repair

The headliner on my Talon fell down during storage. Like most cars of this vintage, the foam between the cloth and the backer disintegrated. This failure allowed the cloth to sag off the backer board.

My dad offered to assist in the repair since he has experience in redoing headliners and other interior parts on vintage cars. He began by removing the sun visors and the dome light held in place by Phillips screws. He then gently pried off the covers over the seat belt tracks. These just snap in place. Next he removed the coat hooks from the B pillars. This allowed the rear trim to be removed.

The headliner board is held in place by several plastic push in pins. These he popped out with the appropriate tool. Once these were out the headliner still sat in the front and rear grooves. He carefully worked it out of the rear groove and then lowered the panel and slipped it out the passenger door.

The cloth came off cleanly but the remains of the foam scatter everywhere. He put the cloth in the washing machine to remove the last bits of the foam. While it was washing, he used a stiff wire brush to scrape all the old foam and glue off the backer board. He then used a vacuum cleaner with a brush attachment to remove the last of the dust. He then vacuumed the dust that had scattered in the interior of the car when the headliner was removed.

Once the cloth was clean and dry, he sprayed a thin layer of prepositional glue on the front edge of the backer. He then worked the cloth into recess for the sun visors and dome light. Because the foam was gone, the cloth was not a little too big and some small wrinkles formed in the recesses. The cloth also stretched some due to handling.

He then worked his way back a few inches at a time smoothing the cloth into place on the headliner backer. In order to get all the wrinkles out he had to stretch the cloth slightly. This caused the holes for the push pins at the rear of the panel to not line up. I considered this a minor problem and ignored it.

To reinstall, we passed the headliner through the rear hatch and slipped it into place in the front groove. We then carefully positioned the side tabs in to the correct recesses. Then we worked the board into the rear groove. Reinstallation was defiantly a two man job as it was difficult to maneuver the large board and work the tabs at the same time.

Once the board was in place we replaced the push pins and the snapped the side panels back in place. The small circles in the cloth at the rear are hardly noticeable and the smooth appearance of the cloth with out the foam looks better than the original to me.

UPDATE: The glue did not stand up to the heat. The cloth separated after being parked in the sun. Will have to try to find a better glue.

UPDATE2: My Dad decided to pain the headliner backer board instead of regluing the cloth. Instead of painting it a solid color he painted the Talon logo. I like the look.

1G DSM Turbo replacement

1G DSM Turbo replacement

My Eagle Talon was showing extreme oil consumption. I noticed that it was worse when I used the boost a lot. I also noticed that on high boost there was a black or blue cloud out the exhaust. The members of DSMTuners forum helped me confirm these were symptoms of a blown turbo seal.

I began trying to figure out which turbo I had. I bought this car used and the previous owner had mentioned the turbo had been modified. However, the turbo had the original marking ground off and some new numbers stamped in their place. I was not able to match these numbers to anything. Once I removed the turbo and disassembled it, it measured the same as a 16G. The stock turbo was a 14b on this car.

My original plan was to put new seals in my turbo. However, one I go tit off the car, I found the hot side housing was severely cracked and pitted. The turbine wheel was also cracked and missing parts of the blades. I am surprised it worked at all.

I found a true Mitsubishi 16G was very hard to come by. So, I decided to take a chance on a cheap eBay knockoff. It came with an installation kit and what appeared to be all the parts I needed. It arrived quickly and I set to work.

I used the procedure from http://vfaq.com/mods/turbo-swap.html to remove the turbo. One addition I have to make is that I had to remove the overflow bottle to get the radiator in and out. This step is not mentioned in the procedure. The idea of leaving the water line attached to the engine worked well. However I had trouble with the oil return line and ended up removing it contrary to the procedure.

Things were going well once I got over the idea that you really have to remove a lot of parts just to get to the turbo. A good pair of hose clamp pliers really helped with all the spring clamps.

I go the turbo bolted to the manifold easily. The kit came with new bolts so I did not have to worry with the stud. I had left the manifold in place like the procedure suggests. I learned the right rotation to bet the turbo in over the water pipe and under the manifold.

My first problem came when I realized I should have installed the oil feed line before mounting the turbo. There was simply not enough room to twist the line in behind the turbo to get it to the fitting. I also noticed that the clip seemed to be on the line backwards. I spread it apart and turned it over. I pulled the turbo back off the manifold and slipped the line in behind the turbo. I then popped out the plastic plug in the top of the turbo and noticed a huge problem. The hole in the turbo was too small for the banjo bolt!

I checked and found it was the right size for the other end of the oil line 10mm not the 12mm that is supposed to be on the turbo end. I tired to think of ways to work around the problem. The only solution I had at my disposal that day was to drill and retap the hole.

I pulled the turbo back off and set up to drill out the hole and retap it to the correct threads. When I got done, I found that my tap would not reach deep enough to thread the bottom of the hole. I needed a bottoming tap that I did not have. I compensated by grinding off the end of the banjo bolt so that it would go in far enough to crush the washers. Only after reassembling everything did I find I had cut too much off the bolt.

I had to pull the turbo back off and order a bottoming tap from McMaster Carr. With the new tap I was able to thread all the way to the bottom of the hole and with a new banjo bolt it screwed in the correct distance. I then put it all back together on the car.

I had a very hard time getting the oil return line back on. The original tube would not pull back up to the turbo after I bent it down to get the turbo out. And the new line was made slightly wrong so theta it did not line up well with the pan. There was a slight twist in the flange. I was able to get the flange to line up by using a pry bar to twist the flange while I started the bolts. I had to remove the down pipe to get enough room to do this however.

When I started the engine there was a huge oil leak at the oil fitting on top of the turbo. I tired new and old crush washers but they all leaked. I even swapped back in the old oil feed line thinking something must be wrong with the new one. I read about annealing crush washers so I tried that. They all leaked.

After buying two more new washers, I carefully examined the pattern on the washers and I noticed there was not full contact all the way around the washer. It was apparent that I had not drilled or tapped the hole straight when I made it bigger. I researched several options and eventually decided to try some nylon washers. The trouble was, the ones I bought had mold marks on them that I did not thing would allow them to seal. I had to sand them smooth before installing them.

The nylon washers sealed. However, now the top of the oil feed line leaked at the head. I removed the bolt to install new washers and I noticed that there was aluminum in the threads. As I suspected, when I tried to retighten it, the threads in the head stripped.

Upon careful inspection, I found that the reason it stripped was that the new banjo bolt in the kit did not have the correct thread pitch. The DSM head is 10mm x 1.25. The new bolt was 10mm x 1.5. Since 10mm x 1.25 is hard to come by, I decided to put in a 1.5 pitch helicoil.

I removed the air box and other items that were in the way of getting the drill in the engine compartment. I pulled the Allen head plug in the front of the head and stuffed in some Q tips to try to limit metal shaving going into the head. I drilled out the hole and then carefully tapped the new threads using the special helicoil tap. I was very careful to make sure it was all straight. I wiped it clean with Q tips and brake cleaner. I then spun the engine over to pump some oil out to flush out the metal shavings.

Once the insert was in place, I was able to bolt up the oil feed line and put it all back together again. This time it all sealed! It took a while to burn of all the oil that had spilled from all the failed attempts.

On the first test drive, I was surprised at how fast the boost came up. Boost comes in much earlier compared to the old worn turbo. I did not make it far done the road before I heard a terrifying noise an the engine died. I coasted to a stop and began looking under the hood. It took me quite a while to notice that the hose had popped off the turbo outlet. Once I put it back, then engine still would not start. I then realized I could not hear the fuel pump running.

I accessed my hidden fuel pump override switch and the engine started right up. After I got it back to the shop and shut it off, the fuel pump operation returned to normal.

The only reaming issue was the temperature gage was not working. I did not realized there were three temperature sensors o the 1G motor. I had made sure the two wires were in place but the sensor for the temp gage is hard to see under the blow off hose. Once I removed the hose and looked, I saw the wire had gotten knocked off. I simply reconnected it and the gage came back to life.

Hopefully this turbo will continue to work well for me. I did some research on the internet and I believe that this turbo was supposed to be for a Subaru and not a DSM. That is why the oil line seemed backwards and the fitting was wrong. I reread the ebay listing and noticed it did not say it was for a DSM. It simply read for “custom applications.”

Dong this project, I added another tap to my collection; I learned how to anneal copper washers and installed my first helicoil. I also learned how to be more patient with removing parts to get to others on the cramped engine compartment of the Talon. I also remembered how much fun this car is to drive.

Pro Comp ES3000 shocks

After doing some research and talking with my brother the mechanic, I decided I would try out the Pro Comp ES3000 shocks for the front on my 1992 Jeep Cherokee. Previously I had purchased the Rancho 5000 shocks, but they only last me about four years which I was very disappointed about.

While I go off roading I don’t go that often. In fact, I have not been off roading at all this year because of my extremely busy schedule with school, kids and the community organization I am involved with. The previous year I had only been off roading maybe three times. From what I was told by other off roaders it would be understandable for my shocks to wear out if I were off roading quite often. So needless to say I decided I was not going to go with Rancho shocks again.

Since I knew there would be a Jeep Fest in Atlanta the first weekend of August I decided I would wait to purchase shocks until after I went there. I wanted to see what was offered and if I could possibly get them at a cheaper price than ordering them online.

When I got there it was ironic that the Rancho booth was right next to the Pro Comp booth which was extremely busy compared to Rancho. I guess that was a sign for me? Plus Pro Comp had a box stuffed full of shock boots including hot pink ones I had been looking for to match the pink my best friend had painted on my D rings, diff covers, track bar and skid plates as well as my brake rotor drums.

After getting in line to talk with one of the sales reps, he recommended the ES3000 shocks which I had previously looked at online. Since I have a 3″ lift he said those were the ones they include in their lift kit. When he told me the price of the shocks I knew I couldn’t turn it down. I would be saving almost $25!

When I went over to pay for the shocks and boots the cashier asked me if I wanted to add the warranty to them. I talked it over with my best friend who agreed that would be ideal. From the way the cashier explained the warranty it seemed like a no hassle deal. $8 additional to add the two year warranty and if anything happened I could take them to the nearest 4 Wheel Drive Parts store to exchange them.

At first the cashier and one of the store managers thought the shocks were in stock at the nearby Norcross, GA store. Once they called though they were apparently not there. I was a little disappointed since I wanted the shocks asap, but when the manager offered to ship them to me for free and said they would arrive to me by Thursday I was okay with that.

So when Thursday rolled around I was out and about hoping my shocks would show up. I had been going to the 4 Wheel Parts website daily to check the status which never seemed to change at all so I was quite nervous that they would not show up. Then late afternoon my neighbor called me and said they had a package for me that was very heavy.

 

When I got home I was like a child at Christmas time. It was a few days before I finally had the time to go out to my best friends house where he has a hydraulic lift and I could install the shocks.

When we opened the boxes he was quite surprised there was some assembling to do. The bar pins had to be pressed in so be prepared if you ever decide to purchase the ES3000. It did not take very long to do the pressing of the bar pins nor installing them.

After two weeks I could already tell a difference in the way it handles and the gas mileage has definitely improved. Now it will be interesting to see how they perform off roading…

 

Leaky Transmission line on a Jeep Cherokee

For at least the last three years every time I have had to put my Jeep on my best friends lift I would always find a little transmission fluid lingering on the upper inlet transmission line towards the bottom of the radiator. Neither one of us could track it down and since it was just a very minor leak we left it alone.

A little over a week ago I noticed something was leaking on the front drivers side about where the steering box is located.    My first assumption was that it was one of the power steering lines at the steering box, but even after cleaning up around everything I still didn’t notice anything. I went as far as wrapping a paper towel around the pitman arm to make sure it wasn’t leaking because it always seemed to be soaked.

 

 

 

 

 

 

 

 

It stayed dry for days so the pitman arm was ruled out. I kept driving it while checking the fluid levels often. Nothing was significantly losing fluids which was puzzling. Then one day after I had picked up my oldest son from school I had went to check my mail when I noticed fluid was almost pouring from underneath.

So, after letting the engine cool down I took the airbox out to clean the steering box up, cleaned the lines and looked over them. That is when I noticed the upper inlet line (transmission line that connects to the radiator) was up against one of the power steering lines. As I cleaned up the line I realized I may have just found the the leak.

When my best friend showed up he pulled the inlet line away from the power steering line and cranked the Jeep up. As soon as he did, transmission fluid sprayed everywhere. In order for me to get it out to his house we had to improvise. I had a left over clamp and he had an old rubber glove which he cut off a piece from. At least it would keep the leak at bay so I could get out there.

 

 

 

 

 

 

 

 

 

 

On the way I stopped at Autozone to special order the upper inlet tube. Luckily there was one at the warehouse in Chattanooga meaning it would be ready to be picked up early the next morning. While there I noticed the leak was still there a little bit.

As you can see in the photo below, it obviously had been rubbing for awhile.

 

I am sure the question one would ask is why was the line allowed to rub against another line? When my radiator was installed there was not a place to attach the clip that holds the line. After I installed the replacement line I had to use wire ties to attach it through a hole underneath the radiator.

The most challenging part of the repair was getting the steel line disconnected from the rubber line even when we were using the transmission line disconnect tool. Using a contact cleaner or something such as WD-40  to get up in there and clean the dirt out makes the difference. With a little effort we were able to finally get it disconnected!

 

As you can see in the picture it was definitely rubbing for awhile.

 

Once I picked up the new line from Autozone for $18.99 it did not take but maybe 10 minutes to install it, add a wire tie to hold it away from the power steering line and re install the air box. No more leaky transmission line 🙂

Taking Care of Your Jeep Cherokee

If you have ever heard someone say Jeep Cherokee’s are tough, they are. Talking to friends and family about their Jeep Cherokees and routine maintenance It was quite interesting to learn how tough they are.

My best friend Mike owns a 1991 Jeep Cherokee Laredo that has over 350K miles on it. Engine and transmission are the originals. However, he informed me it has been close to a year since he changed the oil… He doesn’t even remember the last time he did a tune up either. So the other day he asked me to order a tune up kit from Crown Automotive.

Early in the Spring I ordered a tune up kit from Crown for $45 w/shipping. It comes with six spark plugs, spark plug wires, distributor cap & button, fuel filter, air filter and an oil filter.

Last week I had to order another tune up kit for a friend of mine who owns a 1999 Jeep Cherokee Classic with over 280K miles on it. She and I had spent most of the summer together traveling to Texas then to Michigan into Canada, New York and to Dearborn, Michigan. Between the two trips we put on close to 6K miles in 4 weeks time!  She too couldn’t remember the last time her Cherokee had a tune up.

As you can see from the photo below it obviously been awhile.

Spark Plugs from a 99 Jeep Cherokee Classic

What I usually do during routine maintenance is change the oil, air filter if it is needed. I then check the brake fluid, antifreeze, power steering, transmission fluid, battery and go over the belt and connections. Every other time I will clean the throttle body/idle air control valve. With the tune up kit from Crown Automotive you cannot go wrong. It’s a great way to remind you to get all of the typical maintenance out of the way at one time.