Replacing the Idler Pulley on a Jeep Cherokee

Replacing the Idler Pulley on a Jeep Cherokee

If you get a strange chirping sound from the front of the engine in your Jeep Cherokee it is likely the idler pulley. These have a replaceable bearing but it generally easier to just buy the whole pulley with a new bearing installed.

To change the pulley, you will first have to loosen the serpentine belt. The belt is adjusted at the power steering pump. On most vintages, the power steering pump moves to adjust the belt. On the later vintages, there is an adjuster beside the power steering pump. Removing the air box makes access easier.

With the belt loose, remove the bolt in the center of the pulley. Most have a 15mm hex. Slip the pulley off and remove the sleeve from the center. In most cases you will reuse the sleeve.

If the pulley comes with a new sleeve, use it instead of the old one. Otherwise put the old sleeve in the new pulley. Bolt it back to the engine.

Reinstall the belt and tighten it up. I found the tension is about right when the belt will only twist 90 degrees between the power steering pulley and the water pump. It has to be pretty tight or it will slip when the AC is on.

Dayco No Slack Idler/Tensioner Pulley - 89097

Curing a soft brake pedal on a Jeep Cherokee

Curing a soft brake pedal on a Jeep Cherokee

A soft brake pedal on a Jeep Cherokee can be very unnerving. The brakes are not exceptionally great on a Jeep Cherokee to begin with so when they are not working well, they can be downright scary.

The first place to look on a Cherokee is the adjustment of the rear drum brakes. If the shoes not adjusted right, then the pedal travel required to take up the slack will be enough to make the pedal feel soft.

To adjust the shoes, remove the rubber plug in the backing plate. Use a screwdriver or better yet a brake spoon to turn the spiked wheel. Turn it down to tighten the shoes. I usually tighten them until there is noticeable drag when turning the tire.

If the adjuster does not click when you turn the wheel, then the auto adjuster is likely not installed correctly. I see this problem often. The auto adjuster is operated by a cable the moves the adjuster wheel when the brakes are applied in reverse. The cable is routed over a small metal pivot point. Often the metal piece is not installed correctly under the spring and will allow slack in the cable. To fix, simply remove the spring and reposition the pivot plate in the hole and reinstall the spring. Just make sure the plate stays in place as you reattach the spring. That is the tricky part.

Also, if exposed to road salt, the adjuster screw may seize. Free it up with a rust dissolving oil like PB blaster or ATF. Coat it with grease when re installing to help prevent it seizing.

If the rear brakes are adjusted properly ands the pedal is still soft, you may have air in the lines or a leak. Check the rear wheel cylinders for evidence of leaks. Look for traces of fluid inside the brake drum. In the front, look for fluid around the calipers.

If you still have a soft pedal then you will need to bleed the brake system to purge any air. Air can get in if the master cylinder has ever run dry or if a brake line has been removed for any reason.

I prefer to use a pressure bleed system to bleed the brakes. I find it gets air out faster and I can do it without an assistant. I don’t like using vacuum bleeders because I have found that they can pull air in past aging wheel cylinder seals. If the seal are new this wont be a problem but old ones can allow in air during a vacuum bleed even if they don’t leak fluid out. The old “pump and bleed” method works if you have an assistant but is slower than a pressure bleed.

One last are to look at if you continue to have a soft pedal after checking all of the above is the front brake calipers themselves. Some Jeep calipers use a phenolic piston. The plastic in the piston can break down with heat and start to crumble. If the piston is breaking it may flake off a little each time the pedal is mashed.

Often the brake pedal firmness fades slowly and you get accustomed to it. Once a firm pedal is restored, you may be surprised at how well your Jeep stops and how easy the brakes are to modulate.

Replace windshield wiper bushings on a Jeep Cherokee

How to replace windshield wiper bushings on a Jeep Cherokee

After a while, the windshield wipers on a Jeep Cherokee will develop slack and begin to hit the windshield trim. The Jeep dealer will tell you that you have to replace the entire wiper mechanism. However, the wear is just in the little plastic bushings. With a little know how and some simple hand tools, you can have your wipers working properly again for just a few dollars in bushings.

The bushings you need are available from most auto parts stores who carry the HELP brand. You have to buy a whole pack of wiper bushings to get the three you need.

Begin by removing the wiper arms. There is a small tab near the base of the arm. Pull out on the tab and you can then remove the wiper arm from the splined drive.

Next, remove the several Phillips head screws that hold the cowl cover to the Jeep. Carefully lift the cover up until you can reach the windshield washer hoses. Pull both of these off and then set the cowl cover aside.

Remove the four torx head bolts that hold the wiper mechanism to the Jeep. These are T30 torx. Then, remove the bolt that holds the drive motor to the Jeep. It has a 13mm head. Disconnect the wiring harness from the drive motor.

Drop the splined parts through the cowl and then work the whole assembly away from the center of the Jeep into the cavity in the fender. Rotate the mechanism so that you can lift it up and out of the access hole.

Locate the three plastic bushings in the linkage. Check them for slop. On mine, only the one at the drive motor was worn excessively. Mark the linkage so that you can put it back the way it was. Use a pry bar to separate the bushing from the pivot ball. Place the bushing over a receiving cup. I used a large socket. Tap it with a hammer to remove it from the linkage. Flip the link over and drive in the new bushing in a similar manner. Make sure the tabs are aligned with the slots in the link.

If the pivot balls are rusty, clean them before reassembly. I also added a dab of grease, but that is not required. Press the ball into the bushing. Repeat the process for the other two bushings as needed.

Slip the mechanism into the cavity in the fender and rotate it back into position. Start the drive motor bolt, but do not tighten it. Make sure that the wires and washer hoses are not trapped below the linkage. Install the four torx bolts that hold the mechanism to the cowl. Once all four are started, tighten them all down. Then, complete tightening down the drive motor bolt.

Reconnect the wiring harness. Connect the two washer hoses to the cowl cover. Replace the cowl cover and screws. Slip the wiper arms back onto the splined drives and set the clips.

Spray some water on the windshield and test the wiper operation. Make sure the travel is correct and that there is no binding. If the wipers do not park in the proper position, remove them from the spines and reset them to the correct position.

Dorman - Help Windshield Wiper Linkage Bushing - 49447HELP Wiper bushing kit

Cat back Exhaust for Jeep Cherokee XJ

Cat Back Exhaust for Jeep Cherokee XJ

My old exhaust was crumbling apart. The tip had fallen off behind the holder and the muffler had a huge crack in the bottom. It rattled and rumbled.

Old Rusty exhaust
Old Rusty exhaust

I ordered the Dynomax system from Summit Racing through their Ebay store. It arrived in just a couple of days after I ordered. I had to laugh at the UPS man struggling with the huge box coming in my office door.

Smash checking out the package
Smash checking out the package

I began by lifting my Jeep and using a reciprocating saw to cut the muffler loose from the catalytic converter. There were a lot of old welds here so it was pretty messy. I cut the muffler to get room to work to clean it up.

Cutting off the old
Cutting off the old

The clamp at the rear hanger broke when I tried to unbolt it. I just twisted it out of the way. With both ends loose I was able to remove the muffler and tail pie as a unit from over the axle.

Old Exhaust out of the way
Old Exhaust out of the way

I used a variety of metal working tools to clean up the end of the cat. I cut off the bulk of the old pipes and weld beads with a torch. Then I used a 7 inch grinder to clean up the slag. I finished with my 4 ½ inch grinder fitted with a flap disk.

Old welds gone
Old welds gone

When I finished the reducer include in the kit slipped smoothly and snugly into place on the cat. There was a small hole in the pipe coming out of the cat so I elected to weld this joint closed rather than use the included clamp.

Reducer in place
Reducer in place

Next I slipped the muffler into place. I supported it on a stand while I fit up the tail pipe. It took some wiggling to get the tip to line up where I wanted it between the spring and the trailer hitch. When I finally got it in place I used a ratchet strap to hold it in position while I put a tack weld between the muffler and the tail pipe.

Muffler in place - Jeep Cherokee
Muffler in place - Jeep Cherokee
Tail pipe in position
Tail pipe in position

To get the rubber donut to connect properly with the hanger welded to the tail pipe, I removed the two bots that hold the hanger to the body. Then I slipped the donut over the hanger on the pipe and then I reattached the hanger using the bolts. This seemed easier than wrestling with the heavy rubber, which was cold and inflexible.

Rubber doughnut hanger
Rubber doughnut hanger

I then tightened the clamp on the rear hanger making sure the pipe was still positioned where I wanted it. I then installed the clamps at each end of the muffler. I rotated them so that the base of the clamp would face to the side. This gives maximum ground clearance and protects the ends of the bolts from damage.

Muffler clamped in palce - Jeep Cherokee
Muffler clamped in palce - Jeep Cherokee

With all the clamps in place, I removed the support and gave it a good shake to make sure it was positioned where I wanted it. I then lowed the Jeep and started the engine. I raised it back up and checked for leaks. Finding none, I was ready for a test drive.

Cat back system complete - Jeep Cherokee
Cat back system complete - Jeep Cherokee

The Dynomax system has a nice throaty rumble without being loud. I am very happy to have my exhaust gasses exiting from behind the Jeep again instead of from underneath.

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Rear Wheel Bearing Replacement

Rear Wheel Bearing Replacement – Jeep Cherokee Dana 35

Janice’s 1999 Jeep Cherokee has had a roar in the rear axel for a while now. I finally got around to checking on last week.

I ordered new bearings and seals from Crown Automotive. Since her rear differential is the Jeep Trac Loc, I had to have the friction modifier compound for the grease. I found that at Advance Auto.

I began by lifting the Jeep and removing the rear wheels and brake drums. These had never been off and still had the little clips from the assembly line on two of the lugs. I cut those off with dikes.

Next I let Janice remove the cover. Janice dropped it in the bucket of grease that made quite a mess.

Next I used a 1/4 inch 12 point box end wrench to remove the bolt from the cross pin. I had been concerned that pulling the axles on a Trac Loc diff would be more difficult but it was exactly the same as any other stock Jeep Carrier. I just removed the pin and slipped in the axle to release the C clip.

I removed the left side axle first as it seemed the noisiest. I had a little trouble getting the seal out because the brake shoes were in the way of getting a chisel in like I wanted to. But using a combination of the chisel, vise grips and a seal puller, I eventually popped it out.

I then used an axle bearing puller attachment on my slide hammer to pull the bearing. It takes quite an impact on the slide hammer to get the bearing to move. I have done this job on other Jeeps so I knew to hit it hard. The bearing came out smoothly once it stated to move.

The new bearing seems a very tight fit. I had trouble getting it to start straight in the axle tube. I did not have a bearing driver quite the right size and in trying different ones I somehow damaged the bearing. I noticed some of the rollers missing when I got it in place. So I had to use the slide hammer and pull the new damaged bearing.

I was more careful with the second bearing and got it in with no problem. I put a small amount of Permatex on the outside of the seal and drove it in place. I put a little gear oil on the seal to prelube it.

As I was wiping down the axle shaft to reinstall it, I noticed that there was checking in the bearing race on the shaft. Shaft will have to be replaced. I checked for spares but the only one I had was from a ZJ and the ABS tone ring was different. I replaced the original shaft temporarily.

I slipped it in place and reattached the C clip. I pulled the other shaft and noticed it had some wear as well. I will have to get two replacement shafts along with another bearing to complete the job. I reinstalled the other axle and C clip and coated the cover flange with Black RTV.

After letting the RTV set up for a minute or two, I reinstalled the cover and tightened the bolts in a crisscross manner. Janice refilled the diff with gear oil and the tube of friction modifier.

I later pulled the ZJ axles and looked at how to remove the tone rings. My bearing puller was not long enough to reach. I knew I could use my Dad’s press but I did not want to make the drive to his house.

I did some research on the internet and found a forum post that suggested that the rings would come off easily if heated. Since it was very cold out, I decided it would be a good time to try. The forum post had indicated that the tone ring was aluminum so I was being very careful not to crack it.

I put the axle shaft in the vise and began heating the ring with my acetylene torch. Soon I was able to pry the ring of the seat. I dropped it on the floor to cool. I noticed that it did not sound like aluminum.

I took a magnet to it and found it was indeed magnetic. That made sense to me since the tone ring is used to generate a magnetic field for the sensor to rear the wheel speed. It had to be steel. I was more aggressive with the heat on the second one and it slid off easily without any prying.

These shafts had no visible wear on the bearing races and look like they will make fine replacements. I just have to get more gear oil and another bearing and then find time to do the job again.

UPDATE: I have the spare axle shafts ready to go in but so far the old axles are running quietly. I will just let them run for a while.

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